THIS 31 IS FOR SALE - MAKE A SERIOUS GOOD OFFER AND IT'S YOURS!
cruise around this website for more pictures
Here's an article
about our ProKeys 31H Leslie. As you
can see, this Leslie has been rebuilt, refinished, and has a unique steel caster
plate which allows us to tilt it back and roll it around, something like a huge,
top heavy hand truck. This could be considered a road Leslie, as it goes
out on plenty of gigs. Because of its height, it barely fits inside the
trailer opening though, and it's pretty bulky to move around, but it certainly
sounds wonderful. It uses all original audio components, including a
Jensen F15LL Concert Series Field Coil 15", reconed to exact specs in 1997,
an all original Jensen Hypex V21 driver, complete with its original sealed back
shield, and a stock crossover network. The Type II amplifier has had all
the electrolytics replaced, and is due for some component upgrades and
replacements soon.
When we first got
this Leslie, it was really trashed. Lacquer was peeling off in sheets, it
had white paint on one side, and rust everywhere there was metal. The
motors wouldn't even turn, they were rusted solid. Nothing seemed too
badly broken, but it was in really miserable condition. At first, we
thought of just painting it flat black, but then I got curious what sandblasting
might do to it. After two minutes of blasting, I was glad I didn't paint
it black! The blaster took the finish right off, and "averaged
out" a lot of the scrapes and nicks in the wood. We discovered that
sandblasting isn't nearly as destructive as we first thought. I had
visions of huge holes blasted right through the sides - it just isn't so.
The blaster gun can be held as far away as needed, and you can easily control
how much effect the sand has.
After blasting was
complete, we started planning the addition of two speed motors. Building
the two speed motor mounts was an interesting project, as we discarded ideas one
after another. As you know, the 31 was made with fast-only motors, and the
original metal mounts wouldn't work at all with the larger and heavier two speed
units. I decided to fabricate an upper shelf, along the lines of the later
Leslies. It would still be similar to the original, but larger. I
wanted to mount the upper motors right under the shelf, rather than trying to
suspend them on the inside wall with any kind of bracket assembly. The
first decision was height - we needed a shelf slightly higher than the stock
shelf was, to allow clearance for the taller motor stack with the slow motor
attached. Our final design uses three pieces of 3/4" plywood - a
shelf and two supports. We also added an additional support brace along
the left inside wall of the box. Similar to the original shelf, the new
one is simply a top plate and two end support plates. Openings in the
shelf were needed for the driver and the motor. I used a very small Dremel
router to work on the motor mount area. It was necessary to remove plywood
on the bottom of the shelf, above the motor mount area, to allow the pulley to
clear the top of the shelf. In this 31, the motor is mounted solidly to
the shelf with no rubber shock mounts. Some motor vibration noises are
picked up with this kind of mount, but they're not excessive. Some day,
I'll put some time into redoing this mounting system, and use rubber to isolate
the motors. Once the top shelf started to take shape, the rest of the
project became easier. We used a standard 122 type upper belt tensioner in
the 31, which solved that problem immediately. Spacing didn't allow the
tension spring to be mounted in the same way as a 122, so we mounted it on the
opposite side. By this I mean the belt isn't being tightened towards the
back of the Leslie, it's tensioned towards the front of the cabinet. The
pictures will clarify it better. Looks a little unusual, but it works
exactly the same way.
The lower motor
mount caused a few more problems. We solved them by cutting a
rectangle of plywood, and opening it up for the pulley and motor mounting
bolts. It mounts solidly in the right rear corner, directly to the
existing cabinet corner bracing. This location does NOT match the
length of the lower belt, so we had to design some kind of a tensioning device
for the lower belt. Because the motor is mounted solidly, it can't be
swiveled to make the belt looser or tighter as required. We worked on this
problem for quite awhile, and came up with a strange solution. With the
Leslie laying on its face, we made some measurements in the area that a tension
pulley was required. Unlike other Leslies, the 31 has a wide open bottom
with a steel support bracket across its width. This bracket is the mount
for the lower bearing for the drum rotor. The drive pulley for the lower
drum is mounted below that bracket. I machined a narrow, approximately
1/4", three or four inch slot into this bracket in the correct
location. Then we rigged an old lower pulley onto an axle, using a bolt,
spacer washers, nuts, tubular metal inserts, and some ProKeys
mojo. We bolted this assembly in the slot in the steel rotor support
bracket. It's made in such a way that we can adjust the height of the
pulley to match the belt, and the assembly can slide laterally to make the belt
as tight as needed. The tensioning pulley rotates freely on the
axle. Yes, it really is difficult to adjust the lower belt.
Fortunately, it's held the adjustment for several years now, and only needs an
occasional drop of oil in the tensioning assembly if we hear a squeak.
After we were
satisfied with the mechanical arrangements of the motors, we made a few other
changes to the cabinet. The 31 Leslies used wood screws to fasten the back
panel onto the cabinet. We replaced them with threaded Tnuts and stainless
machine screws and washers. Wood screws were also used originally to bolt
down the 15" speaker. Again, we replaced this system with
Tnuts. But we do this a little bit differently. We mounted the Tnuts
inside the bass compartment, and threaded stainless screws up through the
shelf, from the bottom, using flats, locks, and thread sealer. (see the
next paragraph). This method presents eight bolts sticking up which go
through the mount holes in the speaker frame. Once the speaker is in
place, we use flats, locks, and nuts to really torque it down
solidly. We use this mounting method in all of our Leslies, and never have
loose speakers. I should include a warning here: if you choose to
use this mounting system in your own Leslies, be very careful when you
reinstall the 15" speaker. It's very easy to poke one of those screws
right through the cone if you're not paying careful attention.
Here's a little trick that
you may find pretty useful. In a typical Leslie, there are several screws
threaded into Tnuts, which serve as mounting posts. Examples are the upper motor
mounts and the tensioning arm mount. Very often, these screws work loose,
and their washers cause a vibration noise inside the Leslie when certain notes
are played. I've searched around for weeks trying to track down some of
these noises. And they drive you crazy! Try this: remove the screws,
buy some flats and locks, and when you replace the screws, seal them into the
threads with Hot Stuff or Krazy Glue. They probably won't ever cause
vibration noises again.
Back to the 31H
project - All inside surfaces of the upper and lower compartments were painted
with a semi gloss black exterior paint. The bottom drum rotor was also
painted - it was originally a strange silver color. The paint allows us to
wipe up dust with a damp rag, much easier than raw wood.
A friend of ours
welded the right angle caster bracket. Basically, it's just a steel
"lip" that's attached to the back of the Leslie with two casters
mounted on flanges. We used long and very heavy wood screws into
the sides of the cabinet to attach this plate. The bracket is made so the
casters do not touch the floor until the cabinet is tilted back several
degrees. Because the top of the Leslie is open, (we don't use the upper
back cover), we can grip the top and maneuver it much like a hand truck.
It's very top heavy, and can tilt back on you pretty easily. Currently,
the Leslie does not stand exactly level. The caster plate raises the back
of the Leslie 1/4", so next time we take the Leslie apart, I'll trim
1/4" off the rear "legs" then reinstall.
Finally, we did
some sanding, and finished the cabinet in tung oil. We didn't stain,
seal, or fill the wood, we just wiped tung oil into the open grain. The
end result has plenty of visible open grain and is not glass smooth. Some
people don't like this appearance very much, but in our situation, I think it
makes a lot of sense. Even though we do our best to prevent nicks and
scratches, they seem to happen occasionally anyway. This kind of finish
allows us to do a touch up that blends right in. All that's necessary is
to wipe or spray some more tung oil into the scratch and it seems to disappear
instantly. For Hammonds that travel a lot, I think it's far better than
looking like a battle ax.
We recently
refinished three of our other ProKeys Leslies
using PPG Omni AU, an automotive two part clear coat. Current plans are to
spray this clear finish on the 31, right over the tung oil. The Omni
finish is very hard, resists nicks and scratches, and it's also very
glossy. Sometime soon, I'll take the 31 apart and shoot the clear on
it. Hopefully, there will be no conflict between the two coatings.